Yes sir! Individual baggies, each labeled as Intake 1-4 & Exhaust 1-4.Matt, did you mark and bag the cam buckets/shims for reassembly in the same location? If not, you are looking at valve clearance adjustment and shim purchases.
We took the head off a few days ago, but I was too embarrassed to post anything because of a major blunder. All is well now, so I can "show my face again" and hopefully pay something forward in the process. Following Bryan's removal process, I set up the torque wrench and started on the bolts...snapped one, ugh weird, moved on, ok, then snapped another and my son say's "are you tightening them!" OMG! I was. I literally fell to the garage floor on my knees. The rest came out just fine.
Obviously no one is going to do something as stupid as this, but we have successfully removed two broken off head bolts after HOURS of work, and much frustration. So if it happens during something less stupid, maybe someone can use this thread. One actually came out with those extractor kits (GraBit, etc.), I was shocked. We laid heavy paper across the block surface, moved off TDC, and used washers and duct tape to protect the block if the bit slipped at all (it did, and the washers did the job, no damage). But after a few hours or set up and drilling, it started moving! Came right out. Phew.
Second one, nope, we got it to move one rotation out and then the bit broke off into the drilled hole. Really hard to drill drill-head material (I tried), so we phoned a friend down the road. Pushed the car to his house this morning, he welding a nut to the exposed part, and it came out. Christmas Miracle! If this ever happens again, I am going straight to the weld process, it was faster and higher success potential in my opinion. I read a few posts here that suggested it as well. We had new head bolts on the list anyway, sure...keep telling myself this.
We pushed it back to our house and got to cleaning surfaces. Here are some shots of what we found under the head;
Untouched block, with gasket that looks like wet cardboard & fluid in #4 as anticipated: https://photos.app.goo.gl/2iwcMLoHymN3mWEt6
Underside of the head, more cardboard: https://photos.app.goo.gl/nAFdvz7T2Ec1HjHZ7
The one that needed welding: https://photos.app.goo.gl/JjxoT9bFTYt2xbBUA
Please work: https://photos.app.goo.gl/afCsHaczBALyXBFa7
God is kind: https://photos.app.goo.gl/MYiwbRCmiLBV56ef6
Wiped the block down, nothing more yet: https://photos.app.goo.gl/taMpVSAjJgTSVyBT9
Not really knowing what to expect, things seems fairly clean to me. Time for prep work to clean surfaces and check flatness.
I hope all have a happy holiday!
PS - those washers, I found a video by ELDEST that suggested they are indeed for the hold down screws. Vicks is on vacation, but I'll report back once they respond to my inquiry.
Cheers!
-Matt