It wasn't supposed to be a restoration ....

This is the place to discuss restoration problems, post questions or projects-complete or partial.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

It wasn't supposed to be a restoration ....

Post by axelbaker »

Here is a link to the google drive of photos for any one interested
https://drive.google.com/drive/folders/ ... sp=sharing

This year I decided I needed a toy. Not a full on project, but something fun to drive. So I hunted around a bit and found a 1981 Spider.
It was local, clean, and appeared to be as rust free as I was going to find. The previous owner had done a lot of the aestetic stuff. New top, new interior, new paint (that didn't seem to be covering bondo). Tasteful 14 inch wheels. It ran, sorta. The previous owner though it was something to do with sensors.

Image
So it got towed home.

--

So after getting it home I started on little projects to make it road worthy. Most of them were just cleaning up things left from the previous owner. It got a trunk lock (the previous owner only had an ignition key). I started to clean up the engine bay.. Much of the rubber was old and cracking so it got new rubber under the hood, including al the high pressure fuel lines. I don't know why but some jack ass decided to paint the engine, in the car.

Image

Image

As the investigation continued I started to find some interesting wiring "fixes", including some sort of bypass in the started motor. When removed the started motor would run continuously. After some multimetering and poking I found the "sensor problem" the previous owner suspected. Some genous had cut the ECU and spliced it back on by twisting the wires and electrical taping it. There was actually a short from the ECU to the starter, along with all sorts of other stupid. Amazingly the multirelay was brand new. How did that get replaced and the rats nest of wire splices right next to it not get addressed?!

Image

So out came the fuel injection harness. Just a note here, when Bosch doesn't want you to touch things, they usually tell you in some subtle way. They put a plug in it that's hard to remove like in their AFM's or for wiring, they make it all white. So after studying the diagrams and a multi-metering everything, and soldering and heat shrinking, I had a functional harness.

Image

Image

Image

That done and reinstalled, I tried the motor, and low and behold! It runs! Sounds good! Shit! Let's go try to fail SMOG!
Last edited by axelbaker on Sun Dec 08, 2019 4:10 pm, edited 4 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Time to fail SMOG! or How to make your Fiat melt.

Post by axelbaker »

Well, that didn't work out how I expected. I figured I would try to get smoged, fail, and have a little list of things go to fix. Nope. Passed!!
Well I guess the next thing to do is take it for a drive. Hmmm 24 Hours of Lemons, Hooptie Con, and Radwood is happening at Sonoma Raceway a friend of mine is taking his Bertone Volvo 242. It's supposed to rain. Italian convertible? Let's go!

Image

Image
Me and the Volvo
Image

Image
Image
Even saw a couple other Fiats

The car ran like a champ.
So lessons learned, contrary to popular belief Italian cars do not melt in the rain, and Radwood is awesome!
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Pandoras Sump

Post by axelbaker »

The trip to Sonoma was a success and I drove around and had some fun with the car. I started looking for classic rallies I could do.
I started replacing some of the missing chrome pieces. I found a shifter extension on EBay with a rotted original knob for cheap. The knob was cracked and rotting and fell appart as soon as I touched it. I had a old MOMO from my last car (a 1987 VW Jetta 14 years ago) I planned to use, but it needed refinishing. For fun I decided to see if I could fix the old knob too. Got out the epoxy and ended up with this, Fiat on the left, MOMO on the right.
Image

This is the moment the car became a project.

My neighbor noticed a small oil leak from the sump. Investigation showed an old JB Weld patch job that was failing. So time to drop the sump. Turns out that's a @!$#%$^ pain!

Well no sooner did that cussing stop when new cussing started. I found this in the sump.

Image

That doesn't belong there I don't think. Time for some research.
Oh, that is half of an auxiliary shaft. That's bad.
While pulling off the sump I also discovered some serious cracking in my engine subframe. More welding.
Image
Well that's a good sized project.
Image
Last edited by axelbaker on Mon Nov 25, 2019 1:36 pm, edited 2 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

It should work now right? or I've lost my bearings.

Post by axelbaker »

A lot of cleaning, and a little welding later I had a safe subframe. Hole in the sump got some solder as the welder I have access to doesn't really turn down low enough for thin contaminated sheet steel. A few dollars spend and I had a new aux shaft.
Image
And immediately took a cut of wheel to it and performed a preventative lobectomy.

Image
While I am in there the rod bearings got check, a bit ugly, some of the aux shaft went through. New rod bearings are bought. Let's put it all back together.
Wooohoo! She runs! Again!
Last edited by axelbaker on Sun Oct 27, 2019 7:54 pm, edited 2 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Knock Knock?

Post by axelbaker »

I finally got a chance to drive around a bit. They brakes were the next thing that needed some love. New fluid, hoses, pads and rotors, ordered. What is this?! Why is there an allen bolt in my caliper where the bleeder belongs. Oh! Some genius stripped it. Hmm, fix or replace? Replace.

BIG Thank you to Vick Setaro, he got me a good rear caliper to rebuild for a very fair price.

Fixed! Wait, no. Leaky master cylinder. Ok, Now it's fixed right? So far so go. Let's go have some fun!

And then my luck ran out. Driving home from Berkeley .... knock knock knock. Really?!
Image

Image

Oh! This has got to be my fault. I must have installed the bearing wrong ... or ... I dunno.
Experiment time. What if I clean this up and put in the best old bearing. I haven't got anything to loose right?

Clean the oil galleys, one used bearing, new oil, new filter. Run it. Sounds good. Change the oil. Still good, no sparklies in there.
Sweet!

Though ... But what's that sounds?!
Image
Well that experiment didn't work.
Last edited by axelbaker on Sun Oct 27, 2019 7:07 pm, edited 1 time in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Decapitation time.

Post by axelbaker »

Well, I guess the engine is coming apart. Drain fluids, remove radiator, air box, intake manifold, exhaust manifold, and then the head. Well I did want to get the last of that red paint off the engine. Now's the time.
So how bad are things?
Image

Image
Seen worse.

Image
Before
Image
After.

Image
Exhaust guides knurled and reamed back to spec, lapped valve seats, a little JB Weld to fill some minor pitting, light deshrouding of the valves, broke all the sharp edges, polished combustion chambers, and very light clean up of the intake and exhaust runners. That should be good for 0.01 HP

Image
Image
A little better. Amazing what time and fine abrasives and strategic JB weld can do.
Last edited by axelbaker on Sun Oct 27, 2019 7:50 pm, edited 2 times in total.
Online
18Fiatsandcounting
Posts: 3798
Joined: Fri Mar 15, 2019 11:23 pm
Your car is a: 1969 and 1971 124 spiders
Location: San Francisco Bay Area

Re: It wasn't supposed to be a restoration ....

Post by 18Fiatsandcounting »

Wow, I think the fact that you passed smog and drove around Sonoma Raceway with the engine/car in that condition proves that miracles can in fact occur...! :shock:

-Bryan
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Re: It wasn't supposed to be a restoration ....

Post by axelbaker »

I actually think the cold and wet is the only reason the engine didn't explode.
User avatar
rjkoop
Posts: 976
Joined: Thu Nov 08, 2012 6:45 am
Your car is a: 1981 Fiat Spider
Location: Ottawa, Ontario, Canada

Re: It wasn't supposed to be a restoration ....

Post by rjkoop »

Great read so far... Can't wait for the next installment. :)

Richard
MIGHTY 8
Posts: 307
Joined: Sat Mar 04, 2006 9:55 pm
Your car is a: 1980 Spider
Location: North Chatham NY

Re: It wasn't supposed to be a restoration ....

Post by MIGHTY 8 »

Great reading! Keep the progress coming !
nicks
Posts: 20
Joined: Fri Jan 25, 2019 6:52 am
Your car is a: 1972 FIAT 124 Sport Spider BS1 1608cc

Re: It wasn't supposed to be a restoration ....

Post by nicks »

I'm hooked .... who needs TV !
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Polishing my rod(s).

Post by axelbaker »

With the head off the pistons came out next. Is the number four con rod bent or ovalized? Time for a lot of measuring. Well, after measuring each the big ends on each rod in 5 places, 5 times, and averaging the measurements, then getting nerdy and doing the math again as RMS, I can say .... they are round to with in less than 0.0005" That is my limit of reliable measurements. The pistons and the rings look good too. I guess it wasn't a rod causing the knock.

Well, the rods are out, might as well....
Image

Image

So the connecting rods got their forge lines ground smooth and polished. Then the big and little ends got balanced. I didn't go
too crazy, +/- 1 gram.

Image


My rig to weighing them. The big end goes on the bearings. Worked pretty good.
That should give me another 0.0001 HP.

Join me next time when maybe we finally find out why the motor knocked in the first place.
Last edited by axelbaker on Fri Dec 13, 2019 10:19 pm, edited 3 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

The smoking gun. Or, I still havn't found what I'm looking for

Post by axelbaker »

Well, so far everything in the motor has actually looked pretty good. Nothing has been too far out of spec. Nothing actually explains why it was knocking. I guess I better go do more measuring. So more plasticgauge! This time I went for over kill, one piece every 45 degrees on rod pin 4.

Image

Finally!! A SMOKING GUN!! Some thing that is WRONG!!!

As you can see, on the left we have a piece of unsquished Plastiguage, but on the right there is a piece of squished platigauge. If the rod pin on my crank was round they would be squished the same amount. So my crank is F@#ked!

Well there is only one thing to do about that!
Last edited by axelbaker on Fri Dec 13, 2019 10:21 pm, edited 2 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Exorcise the demons. Or, Back to the grind.

Post by axelbaker »

Image

So the number 4 rod pin had over 0.006" clearance on the top side. It should be less than 0.003" Every thing else showed no wear at all. The nitriding on the crank has held up wonderfully. Better to preserve it.

Image

Off to my friendly local crankshaft shop to get it welded and reground back to spec. Rather than have the whole thing ground undersized (or just rod pin 4) and loose the surface hardness the nitride provided, I chose to just weld the bad pin and grind it to match the others. As a bonus the weld material should be harder and provide a good wear surface.

Sorry, no pics of the reground crank, but it just looks like a crank.
Last edited by axelbaker on Fri Dec 13, 2019 10:23 pm, edited 2 times in total.
axelbaker
Posts: 51
Joined: Fri Jan 18, 2019 2:56 pm
Your car is a: 1981 Spider 2000
Location: Oakland CA USA

Now with more measuring!

Post by axelbaker »

Crank back from the shop I measured every thing again. I have been entering everything in to a spreadsheet. I've tried to document everything, all my clearances, weights when it mattered, etc. So now I can confidently say I have 0.002" clearance on my mains, 0.0025" on my rods, 0.002" thrust. This is the first time I've done a bottom end, I am trying to do anything too stupid.
Image
So, more Plastigauge!

Image

And the paint pen. You can see where the crank was ground in this shot.

Image
Image

Image

Image

If any one is in the market, Midwest Bayless had a great price on an Italian made clutch. About $50 less than every one else.

Image

I opted to install the block with out the head. I don't know how other people do it, but I would rather have less weight to swing around. I also like to use a soft sling or rope for things like this where you can scratch things. I still manage to chunk my paint removing and installing the hood. Next time I pull the hood I will blue tape all the edges on both the hood and the car.
Image
Head back on.

In our next installment we will see if the magic smoke stays inside.
Last edited by axelbaker on Fri Dec 13, 2019 10:15 pm, edited 4 times in total.
Post Reply